Lightning strike, well pump box failed

   / Lightning strike, well pump box failed #61  
A 20 gallon pressure tank should hold 5 gallons of water. When you checked and the air charge pressure was high, that is because the diaphragm is broken and there is water on the air side. Replacing that tank will only get you back to a 15-30 second run time, which isn't long enough. Your pump is working on borrowed time cycling every few seconds like that.

Instead of just replacing the tank, which isn't large enough to limit the cycling, you could add a PK1A and solve the cycling problem once and for all.

View attachment 3318210
Anytime I ever had a bladder leak, water came out the Schrader valve when checking pressure.
I'm thinking bladder tank is 30 gallon since it's not all that much smaller than a 55 gallon drum. I'll check when I have time. I'm working with contractor friend today...house drywall work.
 
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   / Lightning strike, well pump box failed #62  
Like @WinterDeere, I have a fondness for older machinery. I do think that the comment he wrote about temperature dictating duty cycle is spot on.

To unpack that a bit, these days different motors are designed with different grades of insulation, and different temperature ratings. E.g.
Insulation-system-classes-according-to-the-NEMA-and-IEC-60085-classification-15-16.png


There is a bit of a quirk to the NEMA motor ratings in that different intended uses have different service factors (allowed time at maximum current draw). This differs from international norms (IEC). (Full review here for the curious.) However, nearly every modern motor of typical HP that I have seen is at least 100% service factors/duty cycle. Whether the motor will last at 100% is a different call, and gets into the use, and environmental conditions.

Side note: inverter rated motors have higher insulation levels, and often design elements such as square wire, non-random windings, different rotor construction, to function efficiently at frequencies other than 60Hz. (Or 50Hz) Speaking of efficiency, there are also grades of efficiency in motors, and if the motors is in frequent / constant operation, moving to a premium efficiency motor will save energy, and often a short ROI on the added cost.

Back to well pumps; on any given well, one wants to size the pump smaller than the drawn down to keep the pump from running dry, and then large enough to service the expected consumption in a reasonable time period, but short cycling a pump is not desirable which is why there are storage tanks, but neither is a low flow long run, as the submersible pumps need the cooling as @steve tym pointed out, but also due to energy consumption. If you have a pump running against some restriction, like a partially open valve, that is wasted work and energy.

In my experience, pump lifetime gets into usage hours, how it is used, water quality, and especially the presence of foreign matter, e.g. sand, in the water. A pump that gets slowly sandblasted is not going to have a long life time.

All the best, Peter
45 years ago I had water problems but no money. I put gloves on, disconnected pipe and started pulling 1" galvanized pipe. 80ft it looped up over into a pasture & I collapsed!
I took pump all apart and it had this stack of impeller disks that had seized. So I cleaned everything, sanded disks, all back together and tested in tub of water. It worked great!
Back in well and it worked great! For two days!
That's when I put in a new Sears pump, control box and black plastic pipe. It lasted for years, a bad starting capacitor is all I ever replaced.
 
   / Lightning strike, well pump box failed #63  
Sand will certainly shorten the life of any pump. But without pumping sand, it is the motor that determines the life. While running against a partially closed valve is wasted energy, it is no more wasted energy than slowing the pump down with a VFD. And while there is not enough cooling at really low flow when using a VFD, there is when using a CSV. Long runs as low flow do not hurt a submersible. In fact, the low flow reduces amp draw, making the motor run cooler, even at the reduced flow rate. With the drop in amperage caused when the pump is restricted with a valve, it only takes 2/10s of a GPM to cool a 2HP motor or smaller. The 1 GPM minimum built into the CSV is 5 times the flow needed for the motor to last a long time. I have a pump in a well feeding a stock tank that has been restricted to 3 GPM and hasn't shut off since 1996. Pumps like to run 24/7/365, and being restricted to a low flow rate makes them run even cooler.

But a pump submerged in 40 degree water can still overheat, if the water it is pumping is not directed to flow past the motor before going into the pump. In a well that feeds the pump from above, the motor on the bottom can boil water while pumping 56 degree water to the surface. A flow inducer or shroud is important to make sure the flow goes past the motor before going into the pump.

A premium efficiency motor will certainly save energy. But the higher insulation levels, square wave, different rotor construction, and other changes made to motors to run on a VFD are not to make them more efficient at lower frequencies, but rather to help the motor survive the voltage spikes, resonances frequency vibrations, bearing currents, and other problems created by the VFD itself. There is just as much wasted work or energy when slowing a pump down with a VFD as when restricting the flow with a valve.

Water will not come out of the Schrader on top of a tank until the tank is completely waterlogged. But the tank is causing rapid cycling long before water comes out the Schrader.
 
   / Lightning strike, well pump box failed #64  
On a bladder tank, water coming out of Schrader at the top not only indicates a bad bladder, but that the bladder head space has been displaced with water. This would explain the short-cycling of the pump, as without air head, nearly-incompressible water has no volume to displace.
 
   / Lightning strike, well pump box failed #65  
Answer last two posts: yes I made sure ballast tank pressure is ok. Pump is submerged in at least 10 ft of (56°F?) water so shouldn't overheat. Everything seems working fine and not sure how to make it run longer without spending lots of money.
If we open two valves it runs a few seconds...off for (guessing) 1-2 minutes and repeat. Today it's more pressure and volume it seems since I worked on it.
I'm guessing a smaller submersible pump would run longer.
I didn't check fully drained 0 psi tank pressure
It is important to check the air pressure at zero water psi. Other pressures are difficult to interpret.

All the best, Peter
 
   / Lightning strike, well pump box failed #66  
On a bladder tank, water coming out of Schrader at the top not only indicates a bad bladder, but that the bladder head space has been displaced with water. This would explain the short-cycling of the pump, as without air head, nearly-incompressible water has no volume to displace.
True...which is why I said NO WATER comes out my Schrader valve when I check air pressure.
 
   / Lightning strike, well pump box failed #67  
It is important to check the air pressure at zero water psi. Other pressures are difficult to interpret.

All the best, Peter
I'll do that when I get time.
 
   / Lightning strike, well pump box failed #68  
If water comes out of the Schrader valve, the bladder has been bad for a long time.
 
   / Lightning strike, well pump box failed #69  
If water comes out of the Schrader valve, the bladder has been bad for a long time.

Who has water coming out of their bladder tank Schrader valve? I'm just curious to know.
 
   / Lightning strike, well pump box failed #70  

Who has water coming out of their bladder tank Schrader valve? I'm just curious to know.
Common failure mode, but it would take someone REALLY not paying attention to their water pressure, to ignore things long enough to get to that point.
 

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