Routine 1 hour run or more 2021 checklist:
Jan - Feb - Mar - Apr - May - Jun - Jul - Aug - Sep - Oct - Nov - Dec
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Total hours: ~606 on 19 Dec 2021
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Service reminder:
-Change oil on ~700 total hours or/and before July 2022
-Replace valve stem seals, engine is burning oil.
-Replace cracked nozzle heat shielding gasket
-Replace engine rubber mounts (current fix: car tire mount)
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[USER MAINTENANCE]
• Always run at 750W+ load.
• Maximum power: 2.2kW
• Replace oil every 80-100 hours on Synthetic (60hr on Mineral) and every 6 months.
• Clean air pre-filter (foam) with soap and dry every 100 hours
• Recommended oil: (semi/full) Synthetic 5W-40 API CF or CI-4/CJ-4
• Oil crankcase capacity: 1.1L (never overfill; fill above half)
• Wash oil screen filter with Diesel after 4 oil changes.
• Replace air filter every 300 hours.
• Replace oil screen filter every 500 hours. (glue turns brittle overtime)
• Check valves head clearance every 300 hours: Clearance: [0.15mm +/- 0.03]
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[SERVICE MAINTENANCE]
• Replace or clean fuel injector every 1000 hours.
• Optional preventive maintenance : Replace AVR module every 500 hours.
• Re-torque engine head every 500 hours. [42-46Nm]
• Proper Output Frequency (Hz) ~52 idle no load. 50.6 minimum over 1 hour 80% load. 50.4 at 100% (2.2kw)
• Engine Model Name: China clone / Launtop / 178F
Chinese clone of the original Yanmar L70
Approx. fuel consumption (add 10% due to elevation):
https://drive.google.com/file/d/1mZwG8uOWX49wfGSpMrbM-JUSwzZKQjmC/view?usp=sharing
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Manuals
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Clone Engine manual:
https://drive.google.com/file/d/1kZNK0jvYoGCuQwxzJagUdugtsCXqmRBK/view?usp=sharing
Clone Engine Parts List:
http://dieselgeneratorsonline.net/Documents/ETQ170F178F186FPartsList.pdf
Genuine Engine manual:
https://www.nuvair.com/manuals/Yanmar-LV-100-Use-Manual.pdf
Genuine Engine Rebuild guide:
https://cdn.greenmountaingenerators...E-L70AE-L75AE-L90AE-L100AE-Service-Manual.pdf
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Maintenance Logs
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(Nov 2018) Drained stock oil , added Mineral oil for break-in 20 hours 1/3 load ~2400 RPM. 15W-40
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(27 Dec 2018)
Oil refilled with Mineral 15W-40
Old oil non-transparent black on stick
Oil Screen Filter cleaned
Found a very small portion of metal debris on oil filter
2nd break-in 20 hours 80% load 3000 RPM
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(31 Dec 2018)
Changed Oil to 5W-40 Synthetic API SN/CF at 19 hours
Oil Screen Filter was clean
No metal debris on oil filter
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(3 Jan 2019) Adjusted valve lash to 0.15 mm (air intake valve gap was 0.20+, exhaust 0.15+)
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(25 Jan 2019) Adjusted AVR output to 232V from 223V
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(14 June 2019) Changed oil (6mo passed) same oil type.
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(23 November 2019) Changed oil (same as last) at 78hr
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(19 Mar 2020)
Routine valve clearance adjustment (was 0.20-0.25mm on both)
Changed fuel filter
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(4 April 2020) Changed oil (same as last) at 179hr (5month+)
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(12 May 2020)?
Changed Air Filter est. April at 182hr
Vent flexible exhaust adapter mod done. est. April
Added 330ml fuel water stabilizer (WURTH)
Changed governor spring profile to the 3rd hole (see manual)
Readjust. freq = 51hz idle
Increased frequency monitor tolerance relay delay to 1 sec (from 1/2)
Installed genset controller and 186f/178f solenoid flow ctrl injector pump.
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(21 July 2020)
Routine valve clearance adjustment (was 0.20mm on intake)
Injector spray ok
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(5 October 2020) Oil change same as last (5month); filled to -1 diamond level on dipstick
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2020 Aug-Sep-Oct-Nov-Dec 1 hour routine run
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(May 2021)
Oil change same as last (7month) at 234 hr; filled to -0.5 diamond level on dipstick
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(July 2021)
Valve clearance check: intake & exhaust @~0.20mm, adjusted to ~0.15mm.
Fixed oil leak from valve cover old gasket (paper) with grease.
Oil change same as last at 287 hours due to oil leak from cover & close to 60 hours usage
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(Aug 2021)
Changed air filter after 1 year due to flexible exhaust crack (oil contamination) and poor performance. (~100 hour)
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(Sep 2021)
Replaced oil filter on 363 hours
No contamination on filter visible
Replaced oil; 76 hours since last change, same type as last; filled to -1 diamond level on dipstick
Engine rubber mounts damaged, temporarily fixed with mounting the genset on a tire.
Decoupled the wall exhaust with high temperature high flow fan. (Pulls hot exhaust + fresh air for cooling the fan)
Restored the original fuel pump with solenoid valve modification. Last new solenoid fuel pump was failing (unstable rpm)
Replaced feed fuel hose, had cracks (post filter)
Adjusted freq at 50.7Hz warm 50% load
Added 100L fuel (30L existing)
Replaced damaged muffler with 186F large muffler, 178F out of stock
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(Oct 2021)
(400 hours) Engine head retorqued at 42.8 n-m. Front left nut was overtightened, gasket was crushed.
Adjusted valve lash
Added 150ml Diesel 3in1 water stabilizer-inj.cleaner-cetane at 100L
Changed diesel injection timing to advance from 0.5 mm to 0.3 mm; timing shim: 22 degree BTDC, original ~20 (21 standard sea level)
Replaced dead battery and added terminal post connector: 30AH 200A CCA, original 20AH and lug terminal
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(Nov 2021) [Ran on gasoline]
Engine head overhaul due to blown gasket, changed copper o-ring, air intake gasket, exhaust gasket, and rocker arm window rubber seal.
Notes: Pitting on piston head, thick soot layer, cyl. wall surface is good (cross hatch and rough).
Nozzle heat shielding carbon gasket is cracked (FIXME)
Replaced regular tank (150L) with Diesel rated tank (500L)
Replaced fuel filter at total 450 hour
Tested fuel injector spray at total 450 hour (case nut is siezed)
Rassembled original injector pump (non fuel solenoid valve model) due to hunting (non original used for 300 hours, original used for 150 hours at the time of reassembly)
Modifed a servo for throttle lever, and solenoid for lever clutch (shutoff)
Adjusted frequency/RPM to 51.8 at idle hot, 50.6 at 2KW.
Changed oil same as last at 450 hour and at 529 hour (under H level, 1/4 diamond)
Cleaned air pre filter (foam)
Oil pressure sensor replaced due to cracked housing
Valve stem seals burned. (FIXME)
Retorqued engine head for new gasket after 80 hours at 529hr
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(Dec 2021)
Changed oil same as last at 606 hours (80hr)
Only 1/3 of old oil existed, -4 diamonds. No visible leaks.